煤炭工程 ›› 2019, Vol. 51 ›› Issue (1): 40-43.doi: 10.11799/ce201901009

• 施工技术 • 上一篇    下一篇

深厚表土层井壁注浆加固技术研究

张建,朱昌元   

  1. 山东公信安全评价有限公司
  • 收稿日期:2018-02-06 修回日期:2018-04-22 出版日期:2019-01-20 发布日期:2019-03-19
  • 通讯作者: 张建 E-mail:1775763293@qq.com

Study on grouting reinforcement technology of shaft lining in deep and thick overburden

  • Received:2018-02-06 Revised:2018-04-22 Online:2019-01-20 Published:2019-03-19

摘要: 针对张集煤矿副井在井深266~290m接茬处出现井壁出水现象,进行了井壁出水特征和出水机理分析。在井壁出水情况、深厚表土层地质条件及井壁受力分析的基础上,提出了采用壁间和壁后注浆相结合的注浆方案。为尽量减少注浆活动对井壁的扰动,井壁注浆采用诱导注浆和单孔少注、群孔多注的注浆方式,并对注浆顺序进行了设计|然后制定了注浆参数、施工工艺流程和注浆结束标准。通过工程实践证明,注浆后井壁承受的附加应力得到缓释,井壁无渗水,井筒涌水量为0m3/h,说明此注浆方案能够有效地解决深厚表土层井壁出水问题。

关键词: 深厚表土层, 井壁出水, 壁间注浆, 壁后注浆

Abstract: According to the phenomenon of shaft lining water gushing in deep 266~290m summer-planting place of zhangji coal mine auxiliary shaft,the shaft lining water gushing characteristics and water gushing mechanism were analyzed. According to the situation of shaft lining water gushing、geological conditions of deep and thick overburden、on the basis of force analysis of shaft lining,the grouting scheme of in combination with grouting between borehole wall and grouting behind the wall was proposed;in order to as far as possible to reduce the disturbance to the shaft lining of grouting activities,the grouting mode of inducement grouting and Single hole small injection、group hole multi – injection was used,and the order of grouting was designed;then the grouting parameters、construction process and grouting finish standard were developed.Through engineering practice proves, the added stresses of shaft lining were released after grouting, shaft lining no seep water, the shaft lining water gushing was 0 m3/h, indicated that this grouting scheme could effectively solve the problem of the shaft lining water gushing in deep and thick overburden.

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