煤炭工程 ›› 2018, Vol. 50 ›› Issue (9): 43-46.doi: 10.11799/ce201809013

• 施工技术 • 上一篇    下一篇

高水压大断层时效性注浆加固技术研究

刘广超   

  1. 河南工业和信息化职业学院
  • 收稿日期:2018-05-16 修回日期:2018-06-24 出版日期:2018-09-20 发布日期:2018-12-18
  • 通讯作者: 刘广超 E-mail:728626408@qq.com

Study on Grouting Reinforcement Technology of Roadway Passing Through Large Fault

  • Received:2018-05-16 Revised:2018-06-24 Online:2018-09-20 Published:2018-12-18

摘要: 结合九里山矿16061底抽巷揭含水层穿F16-3断层情况,通过布置钻孔探测断层的位置及产状,并在此基础上采用分次成孔、交替注浆的方式对断层进行治理,然后采用“短注短掘、先注后掘”的方式施工巷道。研究结果表明:注浆加固后钻孔涌水量降至0.003~0.30m3/min,有效降低了巷道涌水量|含水层水压由3.5MPa降至0.6~0.8MPa之间,极大的改善了该区域水文地质条件|采用“注10m掘5m”的施工方式,未发生巷道突水事故,巷道稳定性较好。

关键词: 高水压, 大断层, 注浆加固, 导水通道, 双液注浆材料

Abstract: Based on the geological conditions of F16-3 fault in the 16061 bottom lane of Jiulishan mine, the rock stratum in the fault area was extremely broken and the fissure was relatively developed, and there was a great water inrush risk in the course of excavation. Combined with the situation of the mine, the location and occurrence of the fault were determined by arranging the detecting boreholes, and used separate holes and alternate grouting methods to control the fault. The tunnel was constructed by "short injection, short excavation, first injection and excavation". The results showed that: the water inflow from the borehole was reduced to 0.003~0.30m3/min after grouting, thus effectively reducing the water inflow in the roadway. The water pressure of aquifer decreased from 3.5MPa to 0.6~1.3MPa, which greatly improved the hydrogeological conditions of the area. With the construction method of "10m injection 5m", no water inrush accident occured in the roadway, and the roadway has better stability.

中图分类号: