煤炭工程 ›› 2025, Vol. 57 ›› Issue (1): 218-224.doi: 10.11799/ce202501030

• 装备技术 • 上一篇    

全封闭负压连抽高效防喷装置研究及应用

穆朝元,武腾飞,张朝文,等   

  1. 1. 贵州豫能投资有限公司
    2. 河南能源集团研究总院有限公司
  • 收稿日期:2024-07-17 修回日期:2024-09-03 出版日期:2025-01-10 发布日期:2025-03-03
  • 通讯作者: 武腾飞 E-mail:348586795@qq.com

Research and Application of Fully Enclosed Negative Pressure Continuous Pumping and High Efficiency Blowout Prevention Device

  • Received:2024-07-17 Revised:2024-09-03 Online:2025-01-10 Published:2025-03-03

摘要: 为了解决高山煤矿采掘接替紧张问题,通过优化、改进孔口防喷管及防喷三通、“煤渣-水-瓦斯”分离箱、配套研制了螺旋输送装置、行走装置及断电保护装置,形成了具有“孔口-防喷三通-分离箱”多重密封防喷系统的全封闭负压连抽高效防喷装置,并结合钻孔施工工艺,提出了“孔口-防喷筒-分离箱”多重密封工艺,形成了全封闭负压连抽防喷装置施工工艺,实现了钻孔施工发生喷孔过程中的煤渣、水、瓦斯的全封闭治理,并在高山煤矿1907底抽巷进行了现场试验。现场试验结果表明:该装置及其工艺流程实现了打钻喷孔过程中钻渣、水、瓦斯的全封闭治理,有效控制了瓦斯超限,在钻孔发生喷孔时,抽采管路内的瓦斯浓度最高约26%,回风流中的瓦斯浓度最高为0.05%,未出现瓦斯超限情况,在采取安全防护措施的前提下,保证了继续钻进,进尺最大达到60 m/班,提高1~1.5倍|全封闭负压连抽防喷装置能够有效控制瓦斯超限问题,确保了打钻喷孔过程中钻渣、水、瓦斯的全封闭治理,有效控制了瓦斯超限,确保钻孔施工过程的连续性,缩短了瓦斯治理周期,对类似矿井瓦斯治理提供了重要的示范引领作用。

关键词: 高瓦斯, 低透气性, 喷孔, 瓦斯超限, 防喷装置, 瓦斯抽采

Abstract: In order to solve the problems of drilling and spraying holes in the bottom drawway of Alpine Coal Mine, over-limit of gas, long cycle of gas control in the mine, large amount of drilling construction work, which in turn caused the tight succession of mining and excavation, etc., the company optimized and improved the blowout preventing pipe and the blowout preventing tee, the "cinder-water-gas" separating box, and developed the spiral conveying device, traveling device and power-off protection device. By optimizing and improving the blowout prevention pipe, blowout prevention tee, "cinder-water-gas" separation box, supporting the development of screw conveyor, traveling device and power failure protection device, the company has formed a high-efficiency blowout prevention device with multiple sealing and blowout prevention systems, including "orifice - blowout prevention tee - separation box", and has also combined the drilling process to propose a multiple sealing process of "orifice - blowout prevention cylinder - separation box", which has formed a completely closed and negative pressure blowout prevention system. In addition, the construction process of the fully enclosed negative pressure continuous pumping blowout preventive device has been formed, which realizes the fully enclosed management of cinder, water and gas in the process of blowout during the drilling construction, and has been tested on site in the 1907 bottom pumping lane of Gaoshan Coal Mine. The results of the field test show that: the device and its process realize the fully closed treatment of drilling slag, water and gas in the process of drilling and blowing holes, effectively controlling the gas overrun, and when blowing holes occurred in the drill holes, the maximum concentration of gas in the extraction pipeline was about 26%, and the maximum concentration of gas in the return air flow was 0.05%, and there was no overrun of gas limit, and under the premise of adopting safety measures, the continuation of drilling was guaranteed, and the feed footage The maximum drilling speed reaches 60m/shift, which is 1~1.5 times higher; the fully enclosed negative pressure continuous pumping anti-spraying device can effectively control the problem of gas overlimit, ensure the fully enclosed management of drilling slag, water and gas in the process of drilling and spraying holes, effectively control the overlimit of gas, ensure the continuity of drilling construction process, and shorten the cycle of gas management, which provides an important demonstration and leading role for the management of gas in similar mines.