煤炭工程 ›› 2019, Vol. 51 ›› Issue (8): 69-73.doi: 10.11799/ce201908017

• 生产技术 • 上一篇    下一篇

综掘工作面硫化氢涌出规律与治理技术研究

黄立宁   

  1. 中煤科工集团重庆研究院有限公司
  • 收稿日期:2018-12-04 修回日期:2019-01-18 出版日期:2019-08-20 发布日期:2019-09-09
  • 通讯作者: 黄立宁 E-mail:huanglining1983@sina.com

Study on Rule of H2S Emission and Treatment Technology in Fully Mechanized Driving Face

  • Received:2018-12-04 Revised:2019-01-18 Online:2019-08-20 Published:2019-09-09

摘要: 为了降低综掘工作面掘进生产过程中的硫化氢浓度,首先通过现场测试,分析了综掘工作面掘进机割煤过程中的硫化氢涌出规律和沿程分布规律,提出了以“三压带”分段注水工艺技术向工作面预注硫化氢吸收液和截割头高压喷射硫化氢吸收液的治理措施,通过现场试验确定了治理措施的合理工艺技术参数,并对治理效果进行了考察,采取治理措施后距工作面5m、15m处掘进机割煤时硫化氢的浓度分别由269.9×10-6、151.4×10-6降低到27.5×10-6、17.2×10-6,降低效率分别为89.8%和88.6%。

关键词: 综掘工作面, 硫化氢涌出, 预注硫化氢吸收液, 高压喷射, 降低效率

Abstract: Firstly, through field test, this paper analyses the rule of hydrogen sulfide emission and its distribution along the course of cutting coal by road header in fully mechanized driving face, and puts forward the control measures of pre-injection of hydrogen sulfide absorbent liquid to the working face and high pressure injection of hydrogen sulfide absorbent liquid by cutting head with the technology of "three pressure zones". The reasonable technological parameters of the control measures were determined and the control effect was investigated. The concentration of hydrogen sulfide decreased from 269.9 ppm and 151.4 ppm to 27.5 ppm and 17.2 ppm respectively when the road header cut coal at 5m and 15m away from the working face. The reduction efficiency was 89.8% and 88.6%, respectively.