煤炭工程 ›› 2024, Vol. 56 ›› Issue (3): 39-44.doi: 10.11799/ce202403007

• 施工技术 • 上一篇    下一篇

综采工作面超前巷道变形机制及围岩控制技术研究

范红光,卢志杰,蒋东杰   

  1. 1. 河南神火煤电股份有限公司
    2. 河南神火煤电股份有限公司新庄煤矿
    3. 河南工程学院
  • 收稿日期:2023-04-20 修回日期:2023-07-22 出版日期:2024-03-20 发布日期:2024-03-25
  • 通讯作者: 蒋东杰 E-mail:81083584@qq.com

Research on deformation mechanism and surrounding rock control of advance roadway in working face

  • Received:2023-04-20 Revised:2023-07-22 Online:2024-03-20 Published:2024-03-25
  • Contact: JIANG Dongjie E-mail:81083584@qq.com

摘要: 针对采煤工作面超前巷道变形量大等问题, 研究了采煤工作面端部覆岩运动特性对超前巷道变形的影响, 分析了超前巷道切顶卸压机理, 确定了合理的切顶参数, 进行了现场试验。结果表明: 工作面超前巷道的变形的根本原因是工作面推进过程中弧形三角板在工作面推进方向和倾斜方向下沉运动导致其重量及其荷载作用在巷道顶板造成的, 并在此过程引起超前支承压力和侧向支承压力的集中。有效切断回采巷道上方顶板与工作面顶板的联动效应后, 超前巷道替代了单体架棚支护, 超前巷道顶底板累计变形量和两帮累计移近量分别为未切顶的1/5 和1/3。

关键词: 超前巷道, 端部覆岩结构, 切顶关键参数, 巷道围岩控制

Abstract: In response to the problem of larger deformation in roadway advanced of working face, the influence of the movement characteristics of the overburden structure to deformation of the advanced roadway at the end of the working face was studied. The mechanism of roof cutting and pressure relief of the advanced roadway and the key parameters of roof cutting were analyzed, and the field test was carried out. The results show that the root cause of the deformation of the advanced roadway in the working face was the downward movement of the arc triangle roof. The weight and loading acting on the roof of the roadway during the advancing process of the working face. The advanced and lateral stress concentration were the intermediate processes. Reasonable cutting thickness and cutting angle can effectively cut off the linkage effect between the roof above the roadway and the roof of the working face, and cut off the tendency transfer of the advanced pressure. After the application of the research results, the single roof support was canceled in the advance roadway. Compared with that before unloading without roof cutting, the cumulative deformation of roof and floor was 1/5 of the original, and the cumulative displacement of two sides was 1/3 of the original.

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