煤炭工程 ›› 2025, Vol. 57 ›› Issue (7): 60-66.doi: 10. 11799/ ce202507009

• 施工技术 • 上一篇    下一篇

华阳二矿碎软低渗煤层大功率氮气定向钻进试验研究

程卓尔,李泉新,方俊,等   

  1. 1. 煤炭科学研究总院,北京 100013

    2. 中煤科工西安研究院(集团)有限公司,陕西 西安 710077

  • 收稿日期:2024-08-30 修回日期:2024-11-23 出版日期:2025-07-11 发布日期:2025-08-14
  • 通讯作者: 李泉新 E-mail:liquanxin@cctegxian.com

High-power nitrogen directional drilling ina broken soft coal seam with low permeability in Huayang No. 2 Mine

  • Received:2024-08-30 Revised:2024-11-23 Online:2025-07-11 Published:2025-08-14

摘要:

针对阳泉矿区煤层碎软低渗、瓦斯含量高、顺层长距离成孔难、抽采效果差等问题,以华阳二矿为示范矿井,在分析矿井瓦斯地质情况与抽采治理现状基础上,提出了采用大功率氮气定向钻进技术装备进行瓦斯抽采钻孔施工的总体方案,介绍了其技术原理和技术优势,开发了复合定向轨迹控制工艺、复合高效排渣工艺、顺层长距离成孔工艺、定向钻孔长距离筛管护孔工艺等氮气定向钻进关键技术,对大功率定向钻机、制氮装置、大扭矩长寿命气动螺杆马达等大功率定向钻进装备进行了选型,制定了钻场设计、钻孔设计、装备配套、钻具组合等整体试验方案,并在华阳二矿81511进顺钻场进行了顺层钻孔大功率氮气定向钻进试验。试验结果表明,采用大功率氮气定向钻进技术装备可实现碎软低渗煤层内高效定向成孔和瓦斯抽采,施工完成定向钻孔主孔7个、分支孔13个, 其中孔深350m以上钻孔5个,最大孔深506m,,总进尺3363m;成孔直径120mm,全孔下入Φ32mm筛管;试验钻场已稳定抽采超半年,瓦斯抽采浓度均超过50%,最大瓦斯抽采纯量达3.43m3/min,累计抽采瓦斯纯量达68.99×104m3,为阳泉矿区碎软低渗煤层瓦斯区域高效抽采治理提供了新的技术途径,可供类似条件矿井参考借鉴。

关键词: 碎软低渗煤层 , 氮气定向钻进 , 大功率定向钻机 , 制氮装置 , 瓦斯抽采

Abstract:

Aiming at the problems of soft coal seam, low permeability, high gas content, difficult long-distance drilling along the seam and poor drainage effect in Yangquan mining area, taking Huayang No.2 Mine as a demonstration mine, based on the analysis of mine gas geology and drainage treatment status, the overall scheme of gas drainage drilling construction using high-power nitrogen directional drilling technology and equipment is proposed. The technical principle and technical advantages are introduced, and the key technologies of nitrogen directional drilling, such as composite directional trajectory control technology, composite high-efficiency slag discharge technology, long-distance drilling along the seam, and long-distance sieve tube hole protection technology for directional drilling, are developed. The core equipment of high-power directional drilling equipment, such as high-power directional drilling rig, nitrogen making device, high-torque and long-life pneumatic screw motor, was studied and selected. The overall test scheme of drilling field design, drilling design, equipment matching and drilling tool combination design was formulated. The high-power nitrogen directional drilling test of bedding drilling was carried out in the 81511 drilling field of Huayang No.2 Coal Mine. According to the test results, the high-power nitrogen directional drilling technology and equipment can realize the efficient directional drilling and gas drainage in the soft and low permeability coal seam. The construction completed 7 main holes and 13 branch holes of directional drilling, of which 5 holes were more than 350 m deep, the maximum hole depth reached 506 m, and the total footage was 3363 m. The diameter of the drilling hole is 120 mm, and the Φ32 mm sieve tube is put into the whole hole. The test drilling field has been stably extracted for nearly half a year, the gas extraction concentration has exceeded 50 %, the gas extraction purity has reached 2.46 m3/min, and the cumulative gas extraction purity has reached 56.06 million m3. It provides a new technical way for the efficient extraction and control of gas area in broken soft and low permeability coal seam of Yangquan mining area, which can be used for reference in mines with similar conditions.

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